Results 1 to 17 of 17

Thread: Lost another Subaru WRX motor at Mosport GP (big track)

Threaded View

Previous Post Previous Post   Next Post Next Post
  1. #9
    Update on the built motor that failed. I had a tear in the intake duct next to the turbo band clamp, and the clamp was not tight - a maintenance issue.

    Was running lean - and therefore hot - because of this, as you can see by the white in the turbine discharge. We saw the same white on the plugs.

    Coolant and exhaust temperatures seemed normal (196/1100 F) - even at the track - and the intake duct tear never triggered a code (CEL). A little ironic in a way, because I have a Perrin turbo inlet standing by to go on this motor, but never got around to pulling the intake.

    We'll take it apart shortly and I'll give you an update. Hopefully it is salvageable and I can use it as a spare. I seem to need one.
    Attached Images Attached Images
    Laszlo - red '17 WRX
    The all-new Subaru WRX is coming. Pardon our dust.

Posting Permissions

  • You may not post new threads
  • You may not post replies
  • You may not post attachments
  • You may not edit your posts
  •